Winnie the Poo (update: volksworld)

Discussion in 'Show Us Your Ride' started by rob.e, Mar 5, 2014.

  1. Zed

    Zed Gradually getting grumpier

    All the cables should have those, the problem is in 6 months time the tat masquerading as the parts will have fallen apart. I've only ever seen one bus with them from new and it had been owned for 40 years by Lady Something or other, dry stored and used once a year in Cannes after her chauffer drove it there for her while she flew down and back. The rest of the year the chauffer kept it maintained ready for next year.
     
    PanZer, paradox, Lasty and 2 others like this.

  2. I'll have to have words with my chauffeur. .. o_O

    my bus is missing lots of these little parts/ seals etc. i guess i should have expected that when i bought it - PO put this together in a rush. I'm slowly getting there identifying/ sourcing / replacing stuff. those rubber bellows for the throttle cable conduit were 15 quid - for a tiny piece of rubber ffs!
     
  3. DubCat

    DubCat Sponsor

    Search ebay for them. I bought them for pennies.
     
    rob.e likes this.
  4. Zed

    Zed Gradually getting grumpier

    ...per year.
     
    paradox, rob.e and DubCat like this.
  5. Just a quick update on a few things. Steering has been such a pain - original box almost siezed up it was so stiff, N2 engineering box is so much better, like silk lol. New rag joint fitted at the same time.. drag link had a load of play too, replaced that with a new one thinking with these changes i'd be sorted - but no - still cr&p ...ffs!. I have now change the pin and bushings in the beam as well.

    I think.. THINK.. i now have it resolved :D. Need to put some proper miles on it to test fully but my short test run felt pretty good.

    Also just fitted a CSP gear coupling and changed gear box oil. I've had the bus for 9 yrs now and i've not done the gear oil, so its likely well overdue for a change (i think maybe 25k miles?!). Much tighter change and soooper smoooooth :) didn't take any pics so here's one stolen from JK:

    [​IMG]


    "These Urethan couplers are much stiffer compared to original rubber units. The urethane bushings are mounted free of play in the Shift coupler housing made of cast iron. A precisely manufactured solid pin connects the coupler to the shift rod. Will improve overall shifting characteristics. A worn gearbox coupling can often be the cause of a sloppy gearstick. If so, replace it with one of these quality couplings."

    I'd replaced my og sloppy shifter coupling back in 2014 when i first got the bus. I had retained the original cast housing but replaced the pin with a suitable bolt and used the red empi poly bushes that were popular at the time - they were an improvement from what i had then but after 9 years it was getting sloppy. The CSP unit is really well made and the pin fits nice and tight. I can report its much better shifting, much more precise.:thumbsup: For the 30 quid or so these go for it’s well worth changing.
     
    Last edited: Oct 25, 2023
  6. mikedjames

    mikedjames Supporter

    Well worth the extra scene tax.
     
  7. they weren't expensive mike, in fact, prob cheaper than buying some new ones. the horrible old repro's were so badly faded they looked rubbish.
     
  8. I’ve been running an additional little silencer on the end of the pacesetter exhaust to see if I could make the bus a little quieter for the kids on longer trips. Tbh I don’t think it makes much difference and I’m starting to think it’s not a good idea given the additional weight added, plus it’s unsupported so will likely put additional stress on the tailpipe welds.

    so, I took it off.. Replaced by a tail pipe I had in the garage from another project years ago that never got used. Is it too big? Possibly.. :p

    Adds horsepower? Maybe not but it’s definitely increased the ‘burble’ :thumbsup:

    IMG_0280.jpeg IMG_0293.jpeg
     
    Last edited: Sep 19, 2023
    Dubs likes this.
  9. DamonW

    DamonW Supporter

    Looks the business though
     
    rob.e likes this.
  10. mikedjames

    mikedjames Supporter

    I found that swapping the engine bay insulation for modern fireproof 30mm thick high density foam made a difference, along with putting some of the foam inside the tail gate.
     
    rob.e likes this.
  11. pic from Sunday Scramble at Bicester Heritage a couple of days ago.

    53243371953_6ef27b6ef6_k2.jpg
     
    Last edited: Oct 12, 2023
  12. IMG_0380.jpeg

    CSP shifter coupling. :thumbsup: Wired up and with the rubber boot in place.

    Surprised how much difference this has made. Well worth the efforts.
     
    CollyP likes this.
  13. Ian Bell

    Ian Bell Supporter

    Bugger didnt know there should be a rubber boot there...
     
    rob.e likes this.
  14. Main rear seal was replaced a few yrs ago but had started leaking again - looks like i have a groove on the flywheel that shouldn't be there (seal rubbing?) which is probably the cause of the leak. Anyway, new seal is in and nothing showing so far although i've only done 100 miles ish so far. It'll be another 140 or so this weekend to Volksworld show so i'll check again after that.

    IMG_8257.JPG IMG_8255.JPG
     
  15. Lazy Andy

    Lazy Andy Supporter

    See, that’s what Sunday was missing - some cars around the parade ground!
     
    rob.e likes this.
  16. Wow, just realised i missed the anniversary by a couple of weeks - 10 years owning this bay! Blimey.

    Longest i've owned any vehicle.. and its still not finished lol
     
    Chrisd, davidoft and Jean-François like this.

Share This Page