Cold morning

Discussion in 'Mech Tech' started by Adie11, Oct 11, 2022.

  1. So drive my 1600 dual port every week to work . This morning 1st frost . Camper was lumpy and sluggish 1st 10 mins anything I can do to help that ?

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  2. Zed

    Zed Gradually getting grumpier

    10 mins is a long time, there should be enough heat in the heads to run smoothly after less than a minute IMO. If you have choke you should be able to start and drive just fine immediately.
    But you haven't told us one single thing about your carb(s) or distributor so you're not going to get a useful answer.
     
    paradox and Dubs like this.
  3. JamesLey

    JamesLey Sponsor

    If you've got one of these fitted to the carb chuck it in the bin and fit a stock oil bath air filter:
    [​IMG]
     
    Louey, redgaz, Soggz and 4 others like this.
  4. I have solex 34 pic2 and with choke I'm sure I adjusted that the other month as engine wouldn't idle ?

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  5. Have 1 of these but bought a original not oil bath tho as mine 75 just never got round fitting it

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  6. JamesLey

    JamesLey Sponsor

    Fit the original filter in that case. The pre-heat pipe on that will aid in cold weather warm-up.
     
  7. Also check the heat riser pipes from exhaust to manifold are not blocked with carbon.
    Some aftermarket exhaust need the heat riser connections drilling out to allow exhaust gases to reach the manifold
    It sound like your suffering from carburettor icing.
     
    Last edited: Oct 11, 2022
  8. Definitely carb icing ("manifold chilling" would be a better description). Feels like a big flat spot.

    Get the original air filter with warm air feed back in, and that should cure it. I've found the preheat pipes on the manifold (if they're not bunged up with carbon) don't appear to do much.
     
  9. They do with an exhaust that copies the original design so it pulls the gasses through.

    exhausts with both risers just off the connecting pipes don’t work as well
     
  10. The stock design has one heat riser pipe directly off the exhaust pipe near the head and the other to the actual box like this
    ECF13BCF-7937-4440-82E8-3A0E3E4DA24E.jpeg
    most aftermarket exhausts have both directly off the exhaust pipe near the head so the exhaust gasses don’t flow
    Like this
    0B107414-C900-48D9-A43D-8757DA96A70B.jpeg
     
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  11. True. I suspect on the aftermarket 4 into 1s, they're not actually intended to be drilled through - just for show.

    My van originally came with a crap chromy filter and an enormous flat spot. I found just fitting the original airbox, stovepipe etc was enough to cure it.
     
    JamesLey and paradox like this.
  12. Ahem !!you should know by now all sub standard parts like this should not be thrown in the bin,
    They are to be thrown over snottys fence out of harm’s way where they can’t be used again :D

    [​IMG]
     
    scrooge95 likes this.
  13. JamesLey

    JamesLey Sponsor

    One of my favourite dub channels on youtube modified their aftermarket exhaust to more closely match the original. I debated doing it to the baja exhaust but it would've been a bit of a faff.
     
  14. I’ll have a watch of that when I’ve a bit of time to pass:thumbsup:
     
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  15. JamesLey

    JamesLey Sponsor

    Think you'll enjoy his stuff para. A great attitude towards keeping old cars going.
     
    paradox likes this.
  16. Any idea how I can get it to play on the app on my phone instead of on the forum?
    That way it will be in the youtube library so I can watch it later.
     
  17. Just do a search on Youtube for the vid title?
     
    paradox likes this.
  18. matty

    matty Supporter

    just start it off then press the YouTube logo at the bottom
     
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  19. Boom sorted thanks matty
     
    matty likes this.
  20. What I found interesting about that was after the mod so it was more like stock was that he observed lower cylinder head temps on a hotter day than before the mod.
     

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