Backfiring after rebuild

Discussion in 'Mech Tech' started by Honky, Aug 15, 2011.

  1. Could it be the mixture is a bag out ? I tinkered with mine and that did appear to have an impact on backfires, albeit at low revs.........just a thought
     
  2. hailfrank

    hailfrank Admin esq.

    mine did this, checked everthing turned out to be a dodgy electronic ignition. not sure if you run one. have you got a spare points and condensor or possibly another dizzy you could just pop on to test and cross off the list?
     
  3. Valve timing? I had loads of trouble with mine and alot of it turned out to be tappets a bit too tight.
     
  4. Honky

    Honky Administrator

    Tried 3 sperate dizzys with P&C and electronic ignition.

    Carb came from the old engine and has been setup correctly.
     
  5. Woodylubber

    Woodylubber Obsessive compulsive name changer

    yeah im thinking tappets if the carbs set right
     
  6. Honky

    Honky Administrator

     
  7. The sound you describe; backfire as in fuel burning in a hot exhaust. Or. Detonation, fuel air mixture going pop either too late (valve open) or as a result of too lean a mixture?

    In the case of the former, assume the carb's fine, have you checked fuel delivery at the pump? Failing that, fuel pressure too high, or sticking float?

    What is the timing set to at max advance circa 3k rpm?

    In the case of the latter I'd go back to your earlier thought around camshafts. Before that though, one last but unlikely easy fix:- pushrods correctly seated, or rocker assembly incorrectly seated?

    When building the engine if the Cam was seriously damaged this would be visible in the form of pitting or missing surfacing from the lobes, so I'd doubt you'd miss that. One other thing I've seen before is the distributor drive shaft in 180 degrees out. Engine would run, but not at all well.

    Your's on the bench I take it?

    Pedro!
     
  8. Fish

    Fish Administrator

    did you sort this as I may have 2 ideas that aren't covered in replys. let me know.
     
  9. Honky

    Honky Administrator

    We stripped it down and rebuilt with different parts but it would be good to hear your ideas.
     
  10. Zed

    Zed Gradually getting grumpier

    Stuck valve, or as suggested above incorrectly seated push-rods?
     
  11. Honky

    Honky Administrator

    The valve train was my 2nd port of call but it all seemed to be fine.
     
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